| dc.contributor.author | F. Cheers | en_US |
| dc.contributor.author | W. G. Raymer | en_US |
| dc.contributor.author | Ola Douglas | en_US |
| dc.date.accessioned | 2014-10-21T15:53:20Z | |
| dc.date.available | 2014-10-21T15:53:20Z | |
| dc.date.issued | 1947 | en_US |
| dc.identifier.other | ARC/R&M-2355 | en_US |
| dc.identifier.uri | https://reports.aerade.cranfield.ac.uk/handle/1826.2/3433 | |
| dc.description.abstract | A series of tests on an 8.6 per cent thick nose-suction aerofoil designed by Lighthill has been made in the 4 ft No. 2 Wind Tunnel at the National Physical Laboratory at Reynolds numbers of 0.385 and 0.577 x 10(to the power of 6). The results show that the wing stalls at alpha ~= 3 deg (Cl = 1.12) without suction, the lift coefficient at the stall increasing approximately linearly with suction quantity and reaching 1.93 at Cq = 0.019 and 23 deg incidence. | en_US |
| dc.relation.ispartofseries | Aeronautical Research Council Reports & Memoranda | en_US |
| dc.title | Tests on a 'lighthill' nose-suction aerofoil in the N.P.L. 4-ft. no. 2 wind tunnel | en_US |